I have a Openbuilds Blackbox X32.
I have my Grblhal all set,I followed the directions to set it up with Lightburn,
I can Jog and set coordinates and it moves fine.
I should add I have it set to home to the back left, I would like the motors in the back.
When runnin say a simple line, starting at 600 mm finishing at 1000 mm it moves under speed around 200 mm then “stalls” for 20-30 seconds, except its actually moving in the positive direction, then homes back to zero.
What is going on?
I have a Neje max4 and everything works flawless.
I really need to figure this out.
Please someone help me out.
I would try changing baud rate and toggling DTR in device settings.
Thanks for the reply, I will check that out.
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